The purpose of this study is for a company with a great amount of product lead time to reduce the number of its workers and its product lead time by constructing an integrated system, which is formed by the introduction and development of hardware and software in the equipment line of the company. In this study, a company which had a lot of manual processes and therefore needed to stabilize the flow process and the production system for securing technical capacity, was selected. For the purpose of improving the process of the selected company, the present system was analyzed and some sectors which required process improvement were investigated. An integrated system was constructed by introducing and developing software(a CNC design program) as well as hardware(loading/unloading and pallet devices). In addition, the data before processing and the data after processing were comparatively analyzed to see if the process had valid results. The time required and the number of workers required in making the same product were respectively included in the data be-fore processing and after processing. As a method of measurement, a stopwatch method was used and the measurement was done 15 times.